year to year,” says Juan M. Ontiveros,
PE, executive director of utilities and
energy management at UT Austin. “Our
approach was to focus on efficiency. We
needed to meet this growth, but we were
determined to do it in a way that would
pay for itself.”
UT Austin needed to build a new
15,000-ton plant with a footprint
no larger than the 7,800-ton
plant it was replacing.
The UT Austin CHP district cooling
system consists of the central utility
plant (the Hal C. Weaver Heating and
Power Station) plus four chiller plants
with 45,000 tons of capacity tied into six
miles of chilled-water distribution system
piping – the newest of which is located
quite literally in the center of the campus.
In 2004, UT Austin conducted a chilled-water system master plan study, which
determined that the existing plant was
facing hydraulic limitations in the distribution system and was within a few years
of exceeding available capacity. Chilling
Station 2, the oldest plant, consisted of
three steam turbine-driven centrifugal
chillers totaling 7,800 tons. At 50 years
old, it was inefficient and beyond its useful life. In addition, the plant was located
in a prime campus location that was
needed for a new building that would
expand the computer science department.
Faced with this situation, UT Austin’s
utilities and energy management team
members were tasked with building a
new 15,000-ton plant with a footprint
no larger than the 7,800-ton plant it was
replacing. Not only were they faced with
the challenge of a space-constrained
campus, they also had a short project
timeline of two years, from 2007 to
2009. Since the peak campus cooling
load could not be met without the old
station still in service, the new station
had to be ready by May 2009.
“We really hadn’t built a chilling
station from scratch in a very long time,”
says Ontiveros. “Chilling Station 2 space
was needed for an academic building,
but chilling stations are normally very
difficult to replace – just getting the
chiller built takes a year. So we did it as
design-build, only a little differently.”
Due to the time constraint, the
project was implemented as a design-
build project which required the team
to make the chiller selection up front.
Based on a 30-year lifecycle analysis,
and an emphasis on total plant kilowatt-
per-ton efficiency, the following design
elements were identified:
• A 3,000-ton inlet air coil would be
installed adjacent to the new station
to serve the 45 MW combustion
turbine and provide chilled water
from this station to the new 32. 5 MW
combustion turbine that was in
construction to boost generation
capacity and improve the CHP plant
heat rate.
• Variable-frequency drives (VFDs)
would be used on all rotating
equipment to take advantage of the
characteristic that kilowatt-per-ton
efficiency is improved when the
chiller is run at partial loads.
• No control valves would be used to
modulate flow through the chiller
evaporator or condenser to reduce
pressure losses.
• Control valves would only be used
to modulate the three cooling tower
cells so that flow could be balanced
evenly (which would leave only one
modulating valve in the entire system).
Enhanced Control
To ensure that this new chilling
station was able to improve efficiency
and generate savings that created equal
or positive cash flow, UT Austin knew
that it needed to further enhance the
energy efficiency of the total plant. The
university selected OptimumHVAC™
software from Optimum Energy to
help meet these goals. This software
Figure 1. Variable-Speed Performance of 5,000-Ton Centrifugal Chiller at Varying Entering Condenser
Water Temperatures, The University of Texas at Austin.
0.900
0.800
0.700
kW/Ton
0.600
0.500
0.400
Constant;Speed
Variable;Speed
85;F
75;F
65;F
55;F
0.300
0.200
2,000
2,500
3,000
3,500 4,000
Capacity (Tons)
4,500
5,000
5,500